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Title
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Test Section Turbulence in the AEDC/VKF Supersonic/Hypersonic Wind Tunnels
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Date
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1981
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Index Abstract
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Coming Soon
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Photo Quality
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Incomplete
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Report Number
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AEDC TR 81-5
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Creator
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Strike, W. T., Jr.
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Donaldson, J. C.
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Beale, D. K.
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Corporate Author
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Arnold Engineering Development Center
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Extent
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167
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Identifier
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ADA102615
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Distribution Classification
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1
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Contract
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None Given
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DoD Project
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None Given
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DoD Task
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None Given
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DTIC Record Exists
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No
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Distribution Change Authority Correspondence
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None
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Abstract
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Free-stream fluctuation measurements were made in the 40-in. Supersonic Tunnel (A) (at Mach numbers 1.5, 2, 3, 4, and 5) and in the 50-in. Hypersonic Tunnel (B) (at Mach numbers 6 and 8) of the von Karman Gas Dynamics Facility, Arnold Engineering Development Center, using a hot-wire anemometer probe and a dynamic pitot pressure probe. Supplementary surface pressure fluctuation measurements were made on a flat plate model, on the surface of a slender cone model, and in Tunnel A on the stilling chamber and nozzle walls. The results are presented and discussed, and the anemometer and dynamic pitot pressure measurements are compared.
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Report Availability
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Full text available by request
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Date Issued
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1981-07-01
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Publisher
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Arnold Air Force Station, TN : Arnold Engineering Development Center, Air Force Systems Command, United States Air Force
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Provenance
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IIT
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Type
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report