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Title
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A Preliminary Design Analysis of a Multi-Channel Ejector Thrust Augmentation Concept with Oval or Rectangular Air Supply Ducts
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Index Abstract
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Not Available
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Photo Quality
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Not Needed
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Report Number
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ARL 72-0062
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Index Price
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$0.00
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Report Availability
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Full text available
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Creator
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Wright, D. C.
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Allen, J. G.
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Meholick, W. N.
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Salter, G. R.
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Ashby, R.
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Tilyou, C.
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Date
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1972
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Extent
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77
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Corporate Author
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Bell Aerospace Company
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Laboratory
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Aerospace Research Laboratories
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Identifier
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AD0744839
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AD0744839
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Contract
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F33615-71-C-1802
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DoD Project
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7116
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Distribution Conflict
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No
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Access Rights
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Approved for public release; distribution unlimited.
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Distribution Classification
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1
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Date Issued
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1972-05
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Abstract
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The abstract for this report is either unavailable or has yet to be entered
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Date Modified
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Scanned by request 7/1/2020 submitted by a private citizen (Private Citizen)
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DTIC Record Exists
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Yes
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Provenance
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Bombardier/Aero
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Type
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report
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Format
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1 online resource (xii, 59 pages) : ill.
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Subject
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Short Takeoff Aircraft
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Nozzle Area Ratio
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Thrust Augmentation
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Duct Inlets
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Shear Stresses
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Buckling
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Sandwich Construction
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Compressive Properties
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Exhaust Diffusers
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Configurations
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AD Number
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AD 744839
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NTRL Accession Number
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AD744839